Wednesday 28 September 2016

3 years on - Car at work 11 (not Broken down!)

I kind of promised myself not to do these abut two years ago!! But the last month or so has been quite trying  with one thing and another, and I am back to just being very pleased to be able to look down from the same office window at the car park view. Same as three years ago after early dramas when first getting Amy then.

Must realise that it is still quite an achievement, especially since I am doing everything myself so far with only moral support and advice. I have certainly gone beyond what I thought was my capability.

Looking good and similar weather to that date three years ago too!

Monday 26 September 2016

Fuel Gauge working again

The terminal bolt on the sender just span around when trying to undo it, so originally I just pulled the wire off to get the tank out. Didnt think too much of it at the time, but that had screwed up the insulation inside the instrument, causing it to short and give no reading (well.. show full all of the time) I was lucky I didnt spin it arond too much and break the coil wiring, that would have been a difficult repair.

As it happens all I had to do was strip it down, re-insulate the terminal bolt and re-install.

All works fine. Getting an earth is tricky at the moment as I have to drill out the tank bolts to fix it back in properly, and the earth relies on that. Coil to gauge body, gauge body to fuel tank, fuel tank to car body and back to earth. So temporarily I have a wire going from the sender body direct to the main car body, just to bypass any niggles.

Will remove that later when I can. But I know how much petrol I have in the car again!! Actually down at the same amount that was in there when all the breakdowns started happening, so had better fill up now. (and see if the Fuel Sender leaks.. I confess I used a bit of Hylomar to try to ensure not.. more bodge juice!)

Sunday 25 September 2016

Another 15 non stop - tweaks, last steps.

Adjusted timing a little, a bit further advanced. That has made an improvement. Tickover now very nice, acceleration solid, cruising smoother.

Did 15 non-stop, trouble free miles again, just aimlessly around and about. Lots of bitty twisting and turning, but also some nice straight runs to open her up a bit.

Seeming OK so far, ordered a new set of plugs. Shame not to replace them seeing as everything else ignition wise has been replaced. Pop them in this week.

Now I just need to bolt the tank back in and fix the fuel sender so my gauge works again and we are back to normal!! As much as suggestions about further tank cleaning and sealing have been made, I have lost the inclination to do anything more than I have. Hopefully all good, certainly I've done as much if not more than some folks I have talked to would bother with, keep my fingers crossed on that front!

Saturday 24 September 2016

First 25 miles - OK

Relatively uneventful. So far so good! A 10 mile round and round and a couple of slightly shorter round and about.

Cleaned out the carburetor a bit too, tightened manifold bolts. 50 more miles before I need to re-torque the head. Electronic ignition seems fine.

So much done over the past month, almost forgot what has been changed!!

Hoping for the best, why not?!

Amy's history

I applied to the DVLA a few weeks ago to find out where Amy had been. Got some really interesting stuff. Not everything, because they only had centralised records from mid 70's. But it gave me some good info. I have to contact Middlesex if I want older info.

But it was still really interesting. It has enabled me to update some of the info on the About Amy page.

Supporting the restoration date that I had guessed at from an old newspaper I found under the spare wheel, the paperwork confirmed that she was originally Sandringham Fawn and resprayed Green in 1995. So still partially assuming the respray was one of the final acts of a restoration, but 20 years ago seems a fair estimation of when it was done.

Good timing as I was only thinking about that a day or so ago in relation to my fuel blockage issues. Even if the petrol tank was cleaned out then, that's still a while and since the gauze was still in there, then maybe not.

Thursday 22 September 2016

First drive to petrol station - Slosh? Nah....

The internal Slosh sealant arrived today, BUT it is plastered with warnings that preparation is absolutely paramount, the tank needed to be ABSOLUTELY clean and perfectly dry, otherwise the Slosh will fail and need to be stripped out again. The inside of the tank is certainly far better than it was and drying it out is no problem:

First a whole load of sludge came out
When dry, all loads of flakes of rust and stuff came out
The clogged gauze has all but been removed
Then lots of washing out has been done, including with the Tank Kleen that came with the Slosh.

BUT...

It still looks far from clean, very worried that the "Sloshing" would be doomed to failure and would create even more work.

I am in a far better position that previously, so figured that I'd like to avoid it after all.

The upside of that is that the tank is back in, reconnected and with a petrol can full of fresh fuel, I drove her to the petrol station to put in a few more gallons. Just about 3/4 full

Not bolted back in, just held in place by the spare wheel for now.

Will see if any leaks appear (and whether she runs ok now). If not then I will leave it at that. No reason why just a good clean out shouldn't do the trick for a fair few years. That MAY have been the first clean out EVER, or certain since she was originally restored which was at least 10 years ago, probably longer. There was an old newspaper in the boot from 1995, so I'd say over 20 years ago.

Wednesday 21 September 2016

Preparing the outside of the tank

Lashings of red oxide primer!

The remaining underseal was on solid and it was all shiny under what came off, so decided to leave it put.

There was a small rust hole, which I soldered. Can just see the small lump slightly in from the bottom left hand corner as viewed.

Tuesday 20 September 2016

Soldered - no leak

Not the neatest job, but no leak any more. Clean, seal, refit next. Running by weekend? 😎

Monday 19 September 2016

Gauze mostly out

Another poor quality scope picture, but it shows that the feed pipe is now clear.

Also part of what was left of the gauze is photographed here. Totally clogged what was left. Below is the feed pipe coming down vertically above where the drain plug is.





Sunday 18 September 2016

Fuel Tank options and ACCC Barn Day

Cleaning out to one side, this is the issue I have with the tank now:

So I have a number of options to consider.

1) Clean out and repair the existing one I have
2) Buy a replacement one from ebay (there are some available)
3) Get a replacement from the ACCC "Barn"

The third option was put to me on a club night and seemed like a good idea.

I spent a day at the "Barn" with other like minded folks, basically tearing a Somerset apart! But the point being was that I was able to get another tank if I so desired. But the other advantage of being at the day was that there was a lot of experience there. This persuaded me that just repairing the drain plug on mine was relatively easy, they are soldered in, no need for re-welding.

So as it happens the other fuel tanks were just as bad (if not worse) than mine, so I came away empty handed, but with my mind filled with the way to fix my situation.

On that same day the cheap little endoscope camera I had ordered arrived, and i was able to look inside my tank to see what was going on. It confirmed that the outlet pipe gauze was clogged and doing more harm than good. (the camera wasn't very good at pictures though - this is the best I could get:

So cleaning out, re-soldering the drain plug seam, refit tank into car, see what happens..!

That's next. Hopefully fit that in this week, whilst a bit of evening daylight left.

Tuesday 13 September 2016

Fuel tank off!!

Not much else to say! I decided that I need to fix at source and clear the tank. Tried to drain first, using the drain plug, but that was seized and just ended up turning and splitting away. So still need to get it cleaned out but also now needs repairing or source a replacement. So first step - remove from car!




Fuel line completely replaced

So I did that job yesterday evening. There is clear reinforced UPVC fuel line in one run from back to front. The old copper line is left in place, no real good reason to remove it, it may prove to not be the problem at all and will possibly go back to it. It worked for years after all, so it's only a possibly contributor to the problem, not the actual cause, I have to accept that.

The trickiest thing was where to run the PVC line. couldnt follow the copper line as too close to the exhaust. Had to be careful following the chassis due to constant movement of the axle and potential for snagging or even crushing under extreme tilt. (although unlikely, had to consider it)

Ended up like this:



















ACCC night tonight, but no trust to undertake such a journey in the dark even if I get a test drive in earlier in the evening. So I'll be driving Roly and use the opportunity to get some advice if I can. A guy in the club with an A70 Hampshire had exactly this trouble a couple of years ago, so I want to talk it through. Cant remember if he had the tank out in the end or not, that may still be the inevitable answer and I am in denial! Is it such a big job? Not really, it's just having all that petrol sloshing around that makes it a pain.

Monday 12 September 2016

OK - Fuel line still a problem - but clear to see

A few more miles today, mainly to get the engine get warmed up again to give the head gasket a re-torque. But had a couple of errands to run at the same time, so made it a useful journey. Confidence growing in the Electronic ignition, and why not really? If it's working its working.

BUT on the way home suffered a breakdown again. It wasn't the electrics!!!! Although disappointing, the great thing is that now I CAN SEE the problem. The run of clear flexible fuel line showed it was mostly air in the line. When pumping through manually you could see the fuel trying to come through but not managing to keep up.

Blowing back up the fuel line is also easier, and after I did that you could see a "cloud" of dark stuff come back up with the fuel when re-priming manually.

So good news is that it was relatively easy to get going again and CLEAR cause. Bad news is that I am still suffering from intermittent fuel blockage.

Clearly the source of the crud is the tank and I am down to a third full tank and I said I would keep her full. But the run of copper pipe is convoluted and up and down with some sharpish bends, so I will still try the full run of clear line from front to back before I resign myself to needing the tank off. Just in case it is mostly the fuel line getting the occasional block and not from the tank itself. (petrol always seems to flow freely from the outlet... )

I have to laugh when I look back at the day I thought my problem was the spark plugs being loose!! Oh such naive optimism!

Sunday 11 September 2016

Most tentative 2 miles!! - Electronic Ignition in. After over 2 1/2 years!!

Finally, Amy is powered by electronic ignition!! (Originally planned this upgrade in Jan 2014!!)

Took the plunge this morning. It was made rather more complicated by the fact that rotor arm was mounted 180 degrees opposite to the original and the distributor cap is also at 90 degrees to it.

Bottom line was that I had to ignore the instructions to a certain extent and add my own thought process to the HT leads order etc... Only really had to be careful to get no 1 right and then follow the firing order, but nevertheless it hurt my brain at 9.00 this morning!

But after huffing and puffing, it's in and running. Warming up the engine was scary cos it invloved a lot of backfiring to start with, until it was warm then I could take off the choke, do some finer adjustment and then finally around the block. Runs very nicely, although it;s not this magic eureka moment.  But certain aspects are smoother.

I think I'll ask for some help in getting it finer tuned this time from some friends in the club.

There is still hesitation on cruising just like she has pretty much always had. With such a major change of ignition system then it has GOT to be in relation to fuel/carb/mixture or something.

But all good so far!!!

Did another 8 or so miles later on, took a picture, on an  old road near town, whilst meeting up with the family and walking the dog.

Apart from the modern vehicles, it kinda looks old-school as my phone is refusing to focus!! So gave the colouring a bit of a retro feel.






Hopefully can get back to normal now. Will be measuring the miles since these repairs and 20 done so far !! And next milestone is that 40,000 is 500 miles away!

Will refurbish the old distrubutior anyway, I have all the parts to make it good as new. Then I'll carry all of that around with me as my "repair" option!!

Saturday 10 September 2016

First 10 miles!!

This is back to the old days with this blog!! Except no mention of thermostats.

Discovered also that the Distributor was LOOSE, able to move relatively easily. Perhaps it got shoved around when the RAC guy was working on things or when I was doing the head gasket. But it wont help things either and needed to re-set it. Did that visually from old photos. Got her running relatively well and did a drive, gotta start somewhere. Some hesitations depending on speed, but other than that, seems fine.

Haven't replaced any components yet, beyond the condenser that was fitted by the RAC guy.

That's next. Probably take the distributor out to do that and give it a clean up at the same time. Buy wont try to fiddle with the finer timing adjustment until then, no point (!) I don't think.

Pondering the electronic ignition again...! That's only be nearly 3 years after buying it!

Onwards and updwards!

Thursday 8 September 2016

Fuel issues possibly identified and fixed

Fuel starvation was definitely one of my issues, wasn't sure the exact cause, but am reluctant to take the tank out when it may not  be needed. I spotted two things that could have contributed (and explained why I could almost always clear it) The metal braided flexible hose that connected the fuel line to the fuel pump was perished inside and sucking air. Didn't notice before. Also the flexible hose at the rear end that I replaced around a year ago I guess had shrink slightly and had worked itself a little loose and was leaking (so could also suck air)

Originally I was concerned that the fuel line was blocked somehow and I was going to replace the copper line with a straight run of clear reinforced hose, but to start with I am just going to see how things go with this setup:

Shock horror to the purists, I have done away with the braided hose with the Banjo union completely and just connected direct. Surely I'm not the only one to have ever done that bodge??!!

So she's running fine again now, but the ignition system yet to be overhauled. New points, coil, condensor, rotor arm, dizzy cap arrived from the owners club, so bit by bit....!!